matt1995
YaBB Newbies
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Don't let sanity ruin a good adventure....
Posts: 48
Fairfax, VA, USA
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Well,
I kind of figured out the issue. We didn't let the feeler gauge slip all the way into the slot, so we overtightened the valves. We went back, readjusted to .003 and now the bike starts and runs. However, it is not any more noisy (like louder) but the noise has changed to a weird metallic pinging type sound instead of the sewing machine noise it was before. I assumed by adjusting to .003 that we would have quieted the noise more than made it louder. Could we have possibly adjusted on the TDC EXHAUST stroke?
To kind of explain. We turned the fly COUNTER CLOCKWISE, in the same direction as the front wheel turns. We turned it so one set of adjusters went down (away from the adjustment cover), and got the WOOSH out the spark plug hole, then the other, then when the piston came up again, aligned it with the marking. Did we do it right? We didn't have any free play on the rocker arms though, and we tried both on the Compression and the Exhaust TDC strokes and couldn't get rocker free play on either.
I have to do that cam chain tensioner next week (I'm pulling it to send to you) so I will be letting the bike sit anyway, and when installing the new tensioner I plan on readjusting valves again if we did it wrong this time.
PS, the guy I did it with is the guy who will be buying it if I sell it to convert to a Ryca so, it's imperative that we both get it right.
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