DragBikeMike
Serious Thumper
   
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SuzukiSavage.com Rocks!
Posts: 4471
Honolulu
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This completes the carburetor portion of the project. All it took was a little more air filter to get the budget mixer up to speed. I think $28 bucks for the carburetor was $28 bucks well spent. The jetting is dialed in. That budget carb is so sweet I ordered a 36mm to play around with. I’m curious how the two stack up. These carbs might be an excellent solution for the folks who have a mixer that just spent the last two years with fuel in the tank and the petcock left on. One of those beauties that look like the LaBrea Tar Pits.
Let’s take a look at the results using test data from the stock header setup (keeping the project simple & cheap). The setup includes a completely stock engine, PWK38 carb, K&N RD-0710 air filter, modified airbox, catch can, stock exhaust header, LCGP 2.5” resonator with baffle. We have improved the overall performance of the motorcycle. Carburetion is excellent but fuel economy is down by 9.5 mpg. Backfiring has been eliminated. Audible noise has increased a modest amount, but the quality of the exhaust note is more pleasing to the ear. Compared to the box-stock motorcycle, third gear acceleration has improved by 4.71 seconds, and fifth gear passing acceleration has improved by 3.82 seconds (13.73 seconds if you run it all the way up to 5500 rpm).
I think that’s pretty good for such a small investment in time and money. We haven’t done any major work; the engine hasn’t been opened up. Most of us could accomplish these simple modifications for under $350 bucks. The tests show that if you throw on a bigger header it will be a bit faster with no appreciable loss of grunt.
All the easy stuff is done. We have picked all the low hanging fruit and kept a close eye on our bank account. Now it’s time to start doing some open-heart surgery. As I recall, the general consensus was camshaft next. Part 5 will install a DR650 cam.
At this point, I have done 153 WOT acceleration pulls to dial in the different combinations. There’s a little over 2000 miles on the engine since it was restored to box-stock configuration. The old girl is holdin up good. No leaks. No ugly noises. Not using any oil. Zero oil accumulating in the airbox or catch-can. It’s a solid motor.
I hope some of you find this project informative and can use the data I collect to help make decisions on your own project. If you have suggestions or comments on my test methods, post a reply so we can discuss. As mentioned earlier, if you have a particular component or modification that you would like to see included, let me know and we can collaborate. Best regards, Mike
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